This is the second part where I experimented with the new Buwizz components.Since in the last part the control crashed with 2 BuWizz motors on a Buwizz battery box when accelerating too fast, I have now increased the number of Buwizz batteries to 4. Now there were no more crashes. I also disconnected the rear wheel steering from the servo motor and added a few led lights.
![](https://i.ytimg.com/vi/fVePskaVEUw/mqdefault.jpg)